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Last modified
8/16/2009 2:33:56 PM
Creation date
8/5/2009 11:22:18 AM
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Board Meetings
Board Meeting Date
7/19/2009
Description
CF Section - New Project Loans - Farmer's Reservoir and Irrigation Company - Milton Reservoir and Barr Lake Improvements Project
Board Meetings - Doc Type
Memo
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Farmers Reservoir and Irrigation Company Agenda Item 10 <br />July 14, 2009 <br />Page 6 of 8 <br />The schedule for this portion of the Project is: SEO review during July - September 2009, <br />bid the Project in September 2009, start construction in November 2009, and complet e <br />construction by the end of February 2010. The cost estimate for this portion is as <br />follows: <br />TABLE 2 <br />PROJECT COST - MILTON RESERVOIR SPILLWAY <br />Construction $ 834,000 <br />Testing $1 7 , 0 00 <br />Contingency $83, 0 00 <br />Construction Management $ 50,000 <br />TOTAL $ 98 4 , 0 00 <br /> <br />C. Barr Lake Spillway <br />Similar to Milton Reservoir, the SEO’s sp illway evaluation at Barr Lake indicated that <br />its spillway needs to be enlarged to meet State standards. <br />Alternative No. 1 No Action: <br />– This alternative was considered unacceptable because by <br />not increasing the capacity of the spillway, the Company would be ignoring the <br />requirements of the SEO and Barr Lake would likely be put under a fill restriction. <br />Alternative No. 2 (SELECTED) Enlarge the Spillway with a Concrete Control <br />– <br />St ructure and a Downstream Soil Cement Channel: <br />This alternative involved <br />increasing the spillway length . This alternative would meet the Company ’s objective of <br />improving the spillway to safely pass the design storm event as dictated by the SEO. <br />This will allow the Company to continue to operate Barr Lake at its full decreed amount <br />without the concern of dam overtopping. The cost for this alternative was estimated to be <br />$2,1 6 2,000. <br />Alternative No. 3 Enlarge the Spillway with a Concrete Control Structure and a <br />– <br />Downstream Concrete Channel: <br />This alternative involved modifying the existing <br />spillway by expanding it and using concrete lining as opposed to soil cement lining from <br />A lternative No. 2. The cost for this alternative was estimated to be $4,612,000. <br />The Company has chosen Alternative No. 2 because it meets the objective of continued <br />safe operations o f the dam, it complies with the SEO’s directive that the spillway be <br />enlarged, it allow s the Company to continue to store its maximum decreed water volum e, <br />and was the most cost - effective solution. <br />The current spillway, which is an informal low depression, will be widened to 185 feet. <br />The elevation of the new spillway will not be changed. The approach and hydraulic <br />control section of the spillway will be constructed out of concrete. The concrete slab will <br /> <br />
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