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Last modified
7/28/2009 2:40:08 PM
Creation date
4/23/2008 1:57:30 PM
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Weather Modification
Title
Design and Field Testing of a Remote Ground-Based Liquid Propane Dispenser
Weather Modification - Doc Type
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<br />higher than the 11 L/hr desired. (As the flowmeter was <br />inoperable, seeding rates were estimated based on the <br />number of ho~rs of seeding a~d that a fdl tank of <br />proptine \l':as &;seJ). <br /> <br />The SUP?!y line used from the propane tan.1( to <br />the di:-.penser was a 9.5-nun flexible black high pressure <br />hose. It was observed that the hose would absorb heat <br />even at temperatures below freezing causing the propa~e <br />to vaporize in the iiile thus causing line and internal <br />plur.1bing freeze-u? This would render the dispenser <br />inope.av~e. After mid-l\larch it was not possible to <br />release liquid propaae due to this problem. <br /> <br />On Marci. 20, the initial dispenser was removed <br />from the field because of a radio transrr.itter component <br />failure a:id a second dispenser installed. Since seedi:1g <br />could not be initiated from this dispeaser due to supply <br />line freeze-up, orJy communications reliability could be <br />monitored d:.lri~g differe~t weatter conditions. It was <br />deten:lined that racio commuIications even in the worst <br />weatl1cr were excellent. After the second tower was <br />instalkd, conun~nications was never a problem. This was <br />verified by the fact that the station was automaticaHy <br />polled each hour by the computer in Sacramento. The <br />computer kept daily statistics Oil data received (see <br />bottom line in Fig. 7). <br /> <br />Although this first field program was limited in <br />duration it idemified several major design problems with <br />the remote dispenser. These were addressed as <br />described in the foHowing section. <br /> <br />2.2 1989-90 DisDenser Design and Testing <br /> <br />DOlring tl:e S;ltillIler of 1989, several m.ajor design <br />changes were made :0 the dispenser. 1\ot only were <br />there fundamen~al problems with the original design as <br />described above, but there were also problems with <br />performi3g field maintenance with the initi:ll design. <br />This was especially true of the valve aGd plumbing <br />assembly. With the nozzles and valve box separated, it <br />was a major undertaking to replace solenoids or rep~ir <br />leaks in plumbing. Thus the first design change made <br />was to move the valve assembly to the top of the <br />dispenser aGd ta..;e the nozzles protrude from the valve <br />box. This allowed 6e box to act as the shield for the <br />nozzles. In aGdition, ttis allowed removal of the valve <br />assembly without having to remove the supply line from <br />inside the square tubing. Copper tubing was then <br />insura~ed using foam and reflective tape and cor..nected <br />directly from the tank to the valve box at the top of tbe <br />tower completely eliiTinating line freeze-up. Fig. 4 shows <br />the modified valve assembly with supply line attached <br />(uninsulated in this photo). <br /> <br />As a further aid to field maintenance and seeding <br />operations, the original five valves (two for the tanks <br />and one for each nozzle) were replaced with three large <br />filtered lock-off valves (filtering debris in the liquid <br />propaile) to control the three nozzles, Fig. 5. This meant <br />that the two propane tanks would be drawn down <br />together. This not only simplified the plumbing but <br /> <br /> <br />Figure 4 Modified propane dispenser used for the 1990 <br />winter field program. Valve box is now at the top of the <br />tower and acts to shield nozzles from icing. <br /> <br />.r' <br /> <br />----~f_~ - <br /> <br /> <br />~ <br />.;a <br /> <br />~:--- <br />P.:.~ <br />'!"......-- <br /><:: <br /> <br />Figure 5 Valve assembly showing flowmeter in-line with <br />plumbing in foreground and three lock-off valves in the <br />background. <br /> <br />reduced the power drain during operation (each solenoid <br />requires 1 A to operate). <br /> <br />The nozzles were changed to a fiGe spray <br />atomizing type for which Gow rates could be repeatedly <br />obtained of 9.5 to 11.5 L/hr. These nozzles had an irJet <br />diameter of 0.4 mm, requiring internal filters to screen <br />any small particles not fLitered by the lock-off valves. <br /> <br />The antenna design (folded dipole) was changed <br />to ensure antenna integrity during extreme icing events. <br />
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