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<br />, <br /> <br />" <br /> <br />.. <br /> <br />I(+A <br /> <br />Kumar & Associates, Inc. <br />Geotechnical and Materials Engineers <br />and Environmental Scientists <br /> <br />Attachment E, 7 pages <br /> <br />2390 South Lipan Street <br />Denver, CO 80223 <br />phone: (303) 742-9700 <br />fax: (303) 742-9666 <br />email: kadenver@kumarusa.com <br />www.kumarusa.com <br /> <br />=- ~.:::::;:.. <br />~ <br /> <br />Office Localions: Colorado Springs, Fort Collins, Colorado <br />Branch Office: Pueblo, Colorado <br /> <br />April 10, 2003 <br /> <br />Mr. John Gillogley <br />Office of Facility Management Services <br />Colorado Department of Corrections <br />2862 South Circle Drive <br />Colorado SpTings, Colorado 80906 <br /> <br />Subject: <br /> <br />Geotechnical Engineering Evaluation, ReseTvoir Lining System, Rifle <br />COTrectional Center Reservoir No.1, Rifle, Colorado <br /> <br />Project No. 03-1-210 <br /> <br />Dear Mr. Gillogley: <br /> <br />This letter presents the results of a geotechnical engineering evaluation of the <br />perfoTmance of the reservoir lining system for the Rifle Correction Center (RCC) <br />Reservoir No.1, located near Rifle Colorado. The project site is shown on Fig. 1. <br />Seepage analyses were performed to estimate the average permeability of the <br />reseTvoir liner under existing conditions, and the estimated seepage rate if the <br />design permeability had been achieved for the initial and bentonite-amended <br />reseTvoir liner. The estimated, maximum allowable permeability that will allow <br />minimum water release requirements to be met was also evaluated. The possible <br />causes of excessive seepage in the TeservoiT, and Tecommendations for reducing <br />seepage Tates so that water release requiTements can be satisfied are also presented <br />in this letter. The evaluation was performed in accordance with the scope of work <br />pTesented in OUT Proposal No. P-03-200 dated March 3, 2003. <br /> <br />BACKGROUND AND PROJECT DESCRIPTION <br />The existing TeservoiT was constructed in 1998, and has a storage capacity of <br />about 34 acre-feet of water under nOTmal operating conditions. The reservoir was <br />generally formed by excavating up to about 20 feet into a natural hillside, and <br />constructing a homogenous earthfill embankment dam on the downhill side of the <br />reservoir. Based on design drawings for the oTiginal dam prepared by GMS, Inc. <br />(March 1998), the dam generally consists of a homogenous earthfill dam with a <br />14-foot wide seepage cutoff trench extending from 5 to 7 feet below the pre- <br />existing sUTface grade. Clayey soils obtained from the reservoir excavation were <br />used to construct the embankment. The design drawings also show a 12-inch thick <br />sand dTain and collection toe drain beneath the downstream side of the dam. <br /> <br />Based on information provided to us regarding the construction of the dam and <br />reseTvoir IineT, we undeTstand that the oTiginal reseTvoir liner consisted of 12-inch <br />clay Ii neT that was formed by scarifying, moisture conditioning and compacting the <br />upper 12 inches of natural clayey soil exposed at the surface of the excavated <br />Teservoir. Based on the original geotechnical engineering study for the project <br />